Hey guys, its been a while since I've been on here. 2 months ago I had some problems go wrong with my 2000 GP with an XP and top swap. I was so fed up with constantly dumping money in my car so I went out and bought me a 2014 Dodge Ram.....Now...I miss my car so it's time to slowly start trying to fix it. So I was getting on the freeway at open throttle and at high RPMs around 70-80 there was a loss in performance and a weird rattle noise coming from the motor. Bunch of KR and normal coolant temp. I continued driving and it cruised just fine. Tried accelerating a little hard again and same rattle noise. I cruised about 7 miles to work then noticed there was oil spraying out of the front valve cover when the motor was revd. There was no smoke coming out the back. Towed it home and replaced the valve cover the next day. Restarted it and there was still some smoke coming from the rear of the motor, seemed like the Valve cover. At the same time rack and pinion seal busted and dumped fluid all over the ground....that's when I parked it for 2 months. Started the car up for the first time since then the other day and checked the oil...no water, nor milky. Coolant was full before starting it. let it idle for 15-20 min and coolant level stayed the same. No smoke coming from the exhaust. I lightly reved the motor and noticed white smoke coming from the rear and front of the motor. When reving there was white smoke coming out of the dip stick and a little oil seeping out of the front header bolt. Seems like there is some back pressure...made me think of a clogged cat...I put an old one on no more then a month before crap hit the fan, which the cat was sitting on the side of my house for quite a while. Needed it for emissions. Before the major problems I was having some studdering during hard acceleration. Could a clogged cat cause this much back pressure to blow out my gaskets? I was thinking the head gaskets possibly blew too. I am going to unbolt my exhaust underneath like running open headers and see if smoke is still coming out of the motor when reved.

Any suggestions of what I should do or check????
Thanks guys.