Thread: drivability "issue"

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  1. #1 drivability "issue" 
    GT Level Member riceburner's Avatar
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    so i got a ? for people real quick on drivability. when i turn the car on "cold start" it has a rough idle, and the low coolant light is on. after a min or so the idle smooths out and after about 4 min the low coolnt light goes out...? anyone haved any ideas? haha sometimes it will idle fine too i dont even know...
    '01 GTP mods: K&N intake, autolite 104's, drilled 180*, !u-bend, !EGR, ported s/c, polished heads and TB and a LOT more whine
    '99 firebird mods (1 of 6): LS1 swap, custom exhaust, LS6 IM, RA intake, and a few suspension parts
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  2. #2 Re: drivability "issue" 
    DUI BABY Bio248's Avatar
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    my car idles really really bad on a cold start, almost like it has a vacuum leak but it doesnt. never heard of the low coolant light for only a short period..your coolant full?

    either way if it doesnt idle bad when warm, it shouldnt be a driveability issue.
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  3. #3 Re: drivability "issue" 
    GXP Level Member Iron Indian's Avatar
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    If your low coolant light is coming on you have one of two problems... Either you coolant is low and/or needs to be bled properly. OR You coolant sensor in your radiator is clogged with **** from dexcool. Remove, clean well and reinstall...
    Shawn W. Larsen

    2005 Pontiac GTO 6.0 LS2/A4... Stalled/Cam Only: 406 RWHP , 370 RWTQ

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  4. #4 Re: drivability "issue" 
    GT Level Member riceburner's Avatar
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    coolant level is as full as i can get it. let it run open for 5 min with a drilled therm filling till i would not take anymore...and i fouund out today that im throwing a cyl 4 misfire as well as all the egr codes from removing it....would the egr mess the engine up when removed and cause this misfire? i checked and am getting proper spark and injection pulse. engine seems to run ok stutters a bit under heavier throttle and has an idle around 700-800 prm...
    '01 GTP mods: K&N intake, autolite 104's, drilled 180*, !u-bend, !EGR, ported s/c, polished heads and TB and a LOT more whine
    '99 firebird mods (1 of 6): LS1 swap, custom exhaust, LS6 IM, RA intake, and a few suspension parts
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  5. #5 Re: drivability "issue" 
    GT Level Member riceburner's Avatar
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    ttt?...
    '01 GTP mods: K&N intake, autolite 104's, drilled 180*, !u-bend, !EGR, ported s/c, polished heads and TB and a LOT more whine
    '99 firebird mods (1 of 6): LS1 swap, custom exhaust, LS6 IM, RA intake, and a few suspension parts
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  6. #6 Re: drivability "issue" 
    The Blue One blueguy's Avatar
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    Ummm...misfire means one of your spark plugs are bad...PROBABLY #4

    Get rid of that damned drilled T-Stat too...and just get a regular 180*...or 160* whatever you want. Is your EGR removed? If so You would need a block off and a deleted code from the PCM for it to run correctly...but I'd change the plugs and T-Stat first
    Sold WBody's: '03 Blue GTP/'98 Green GTP/'98 Silver GT/'05 GXP
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    '04 Chevrolet Corvette MRM A4/LS1 - TSP LT's, 3"O/R X, AFE S2 CAI
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  7. #7 Re: drivability "issue" 
    GT Level Member riceburner's Avatar
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    the plugs were replaced with this last rebuild. maybe 6 hours on them?...how could it be fouled this fast?!? and whats wrong with a drilled stat? i personally like the idea...and how bad will the engine run till i can get it tuned out? and i have both side of the egr pluged off.
    Last edited by riceburner; 02-04-2009 at 02:23 AM.
    '01 GTP mods: K&N intake, autolite 104's, drilled 180*, !u-bend, !EGR, ported s/c, polished heads and TB and a LOT more whine
    '99 firebird mods (1 of 6): LS1 swap, custom exhaust, LS6 IM, RA intake, and a few suspension parts
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  8. #8 Re: drivability "issue" 
    DUI BABY Bio248's Avatar
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    a drilled thermostat is always a good idea since it allows a little to seep by all the time which keeps cold coolant in the engine more. why would you want to switch to a normal one?
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  9. #9 Re: drivability "issue" 
    GT Level Member riceburner's Avatar
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    the drilled t-stat is staying.....back to the issue?... what would be some causes for a misfire?...and would removing the egr cause the engine to run rich and run funny?
    '01 GTP mods: K&N intake, autolite 104's, drilled 180*, !u-bend, !EGR, ported s/c, polished heads and TB and a LOT more whine
    '99 firebird mods (1 of 6): LS1 swap, custom exhaust, LS6 IM, RA intake, and a few suspension parts
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  10. #10 Re: drivability "issue" 
    DUI BABY Bio248's Avatar
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    the EGR is only active during cruising, so that takes that out of the loop unless youre misfiring while cruising.

    is it just a random misfire? mine seems to do it at idle all the time, but once i drive it is normal. i also havent changed my plugs in a while.
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  11. #11 Re: drivability "issue" 
    GT Level Member riceburner's Avatar
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    it did not say random misfire...
    '01 GTP mods: K&N intake, autolite 104's, drilled 180*, !u-bend, !EGR, ported s/c, polished heads and TB and a LOT more whine
    '99 firebird mods (1 of 6): LS1 swap, custom exhaust, LS6 IM, RA intake, and a few suspension parts
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  12. #12 Re: drivability "issue" 
    GT Level Member Clar2478's Avatar
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    plug wires or coils
    Call me Brad

    '06 GT: Just a few mods here and there.
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  14. #14 Re: drivability "issue" 
    GT Level Member riceburner's Avatar
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    well, the car cruises fine. its just at idle on a cold startup and at wot. at wot it seems to studder a lot and there is no power behind it. and if it were the coils wouldnt the entire 1-4 coil be messed up causing a misfire in two cly instead of just one?
    '01 GTP mods: K&N intake, autolite 104's, drilled 180*, !u-bend, !EGR, ported s/c, polished heads and TB and a LOT more whine
    '99 firebird mods (1 of 6): LS1 swap, custom exhaust, LS6 IM, RA intake, and a few suspension parts
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  15. #15 Re: drivability "issue" 
    I live here. GTPJOE90's Avatar
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    no way the exact thing thats wrong with it is your lacking a spark from the flux capacitor go to autozone ask for fluz capacitor links. problem solved.
    hogan 3inch DP u bend delete ,180*tstat, autolite 104s, LED interior, 4" FWI, 2000watt system, bullitt rims, zzp pistons, pems, alt rewire, thrush muffs, 3.4 zzp mps, transgo shift kit, triple edge performance trans. autometer triple pod :SOON: urlosn HPT PCM tune, HEADERS, 1.9's
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  16. #16 Re: drivability "issue" 
    GT Level Member riceburner's Avatar
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    well i got a new flux capacitor on order from kalecoauto.com

    you pain in the butt! haha i will have money to get new links tommorrow when i get paid.
    '01 GTP mods: K&N intake, autolite 104's, drilled 180*, !u-bend, !EGR, ported s/c, polished heads and TB and a LOT more whine
    '99 firebird mods (1 of 6): LS1 swap, custom exhaust, LS6 IM, RA intake, and a few suspension parts
    Reply With Quote  
     

  17. #17 Re: drivability "issue" 
    GT Level Member riceburner's Avatar
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    i put in the new link and there is still a code? does it need to be reset?...or will it continue throwing the code till it is fixed?
    '01 GTP mods: K&N intake, autolite 104's, drilled 180*, !u-bend, !EGR, ported s/c, polished heads and TB and a LOT more whine
    '99 firebird mods (1 of 6): LS1 swap, custom exhaust, LS6 IM, RA intake, and a few suspension parts
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