Hey dude watever ur problem is good luck w ur issue. After my lil adventure just make sure to use that red anaerobic crap to seal everything back up if u do end up using the one u took apart before. This time I also used a 16oz rubber mallet to make sure all the major parts connected up WELL. I also thoroughly cleaned the mating surfaces. I had an issue with some noise & initially thought it was the coupler. Funny since I've had the green ZZP one since '09. Wasn't the coupler. It was in EXCELLENT shape. Most of the SC oil was gone. I have no idea where the f*ck it went. Doesn't seem like it leaked out. SC gasket is clean & I didn't smell the animal fat BBQ when I would drive. Think some assh*le may have siphoned it out ;D There was a slight leak after reassembly 3 or so weeks ago but I was certain that I sealed it up. Maybe it slowly seeped out then evaporated as I drove each day. So I reassmbled everything, used the Permatex sh*t insted of Ultra Black RTV (never had an issue b4 w that), filled it up w SC oil, then let it set on top of a brick for a few hours. No leaks 36 hours later. Much less noise. Boost behavior seemed a lot better today. Maybe I had a Boost leak where the blades section connects to the other side of the rotor pack.