Thread: Good run, gone bad

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  1. #1 Good run, gone bad 
    I live here. UR LOSN's Avatar
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    well, I met up with Bio today up in Wisc. We had a few runs. 1st 2 we were neck and neck..with me pulling a little on topend.

    The last one I think I jumped the gun by a split second.. but I pulled a car?

    I turned around to come home. I get 14miles down the road, cruise control set at 80mph, sunroof open, windows down, stereo going.... THEN

    WWWHHHHHHHHHHOOOOOOOOOOOOOOOOSSSSSSSSSSHHHHHH!

    nothing but smoke out the back of the car, and a high pitched squeel from the motor.

    I believe the head gasket went, and well coolant in oil spun the bearing... I drove. literally 45 miles limping the car home. coolant stayed at 180... motor smoking like a fire.

    I pull it in the garage. I pull the dipstick. oil on the very tip..so it was burning it. coolant tank was all oily/coolant mix.

    looks like I have to put my spare motor in.

    The 2000 GTP is STOCK other than a tune, Wizair CAI, and 3" DP. I hadnt put on the blower/pulley/rockers yet. She had stock boost. I'm kinda glad I didnt put everything on it yet.

    anyone else have tis problem? she just turned 102thou......
    Last edited by UR LOSN; 03-14-2009 at 08:53 PM.
    2001 GTP- PT76 turbo, Intense Drag cars old engine, Stage 4 Intense turbo cam,FMIC,150 wet,Double roller timing chain,Diamond forged coated pistons 8:0:1,Diamond piston rings,Cryoed L32 connecting rods,Cryoed crank,Clevite77 main bearings,Clevite77 cam bearings,Clevite77 L32 rod bearings,ARP Everything, Intense/meizere true billet Flexplate,Intense Wilson UIM/LIM,Intense oil pressure kit,Cometic,OE-R lifters,Cryoed L67 block,ATI turbo dampner,80# inject,Weldon 2035 fp,Aero Fuel Rails,AL cradle
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  2. #2 Re: Good run, gone bad 
    GrandPrix Junkie Sabrewings's Avatar
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    Looks like Bio got his revenge...
    2004 Impala LS - got some mods sold!!!
    2009 Subaru Impreza WRX STI

    NAIOA moderator Still Imp'n, just in a different Imp.
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  3. #3 Re: Good run, gone bad 
    I live here. UR LOSN's Avatar
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    the funny thing is he was talking like his car was going to blow up. lol. I guess he gets the last laugh!
    2001 GTP- PT76 turbo, Intense Drag cars old engine, Stage 4 Intense turbo cam,FMIC,150 wet,Double roller timing chain,Diamond forged coated pistons 8:0:1,Diamond piston rings,Cryoed L32 connecting rods,Cryoed crank,Clevite77 main bearings,Clevite77 cam bearings,Clevite77 L32 rod bearings,ARP Everything, Intense/meizere true billet Flexplate,Intense Wilson UIM/LIM,Intense oil pressure kit,Cometic,OE-R lifters,Cryoed L67 block,ATI turbo dampner,80# inject,Weldon 2035 fp,Aero Fuel Rails,AL cradle
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  4. #4 Re: Good run, gone bad 
    GrandPrix Junkie Sabrewings's Avatar
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    Point taken. The next time I race someone and they start talking about how their car might blow up, I'm decking them. That way mine doesn't blow up.
    2004 Impala LS - got some mods sold!!!
    2009 Subaru Impreza WRX STI

    NAIOA moderator Still Imp'n, just in a different Imp.
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  5. #5 Re: Good run, gone bad 
    Donating Users BADAZGTP's Avatar
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    Sorry to here that man.
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  6. #6 Re: Good run, gone bad 
    GXP Level Member ryangtp89's Avatar
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    thats too bad hope you get everything taken care of asap!
    SLP headers, Wizaird cai, zzp1.0pcm ,slp powerflo catback, 3.4mps, NGK TR55's, 180*, zzp stage 1 hv tb,tb spacer, tb heatshield, Triple Edge Performance High performance Tranny, flipped motor mounts, spring blockers, prj 10.4mm wires, Sloted rotors & Ceramic brake pads,Alternator Voltage Booster. zzp 1.9 rockers & 105# springs
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  7. #7 Re: Good run, gone bad 
    Donating Users blowfishRus6's Avatar
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    that sucks man! on the upside you beat bio
    white 04 comg G gtp. wizair, pacesetters, slp 1.8 rr
    its slow.
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  8. #8 Re: Good run, gone bad 
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    That's crazy. Looks like you've got some work ahead of you.
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  9. #9 Re: Good run, gone bad 
    I live here. UR LOSN's Avatar
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    eh. I've decided to part it out.... I'll buy a new car sooner than I thought.
    2001 GTP- PT76 turbo, Intense Drag cars old engine, Stage 4 Intense turbo cam,FMIC,150 wet,Double roller timing chain,Diamond forged coated pistons 8:0:1,Diamond piston rings,Cryoed L32 connecting rods,Cryoed crank,Clevite77 main bearings,Clevite77 cam bearings,Clevite77 L32 rod bearings,ARP Everything, Intense/meizere true billet Flexplate,Intense Wilson UIM/LIM,Intense oil pressure kit,Cometic,OE-R lifters,Cryoed L67 block,ATI turbo dampner,80# inject,Weldon 2035 fp,Aero Fuel Rails,AL cradle
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  10. #10 Re: Good run, gone bad 
    DUI BABY Bio248's Avatar
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    dude that bites. you got a scan gauge or anything? were you knocking at all? if coolant was in the oil and oil was in the coolant then it probably was a head gasket. if you would have been closer to home and not actually drove it home there may have been a possibility to save it, but that squeal makes me think the bearing went because the head gasket was already gone. i didnt notice any smoking when we were running or i would have said something to you. the last motor i had that spun a bearing did the high pitch squeal thing too then it started knocking at idle (KR) and i couldnt keep the car running for the life of me. it would die just cruising.

    it just seems awkward that it would have been running fine up until that point. it is almost like the head gasket was gone as you were driving up. my pops always told me that cars run the best when they are on their last leg.
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  11. #11 Re: Good run, gone bad 
    I live here. UR LOSN's Avatar
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    nope, no knock.... no signs of it was going to let go. it just went.


    well. for having less mods, and more people in the car...

    It must have been on its last leg. It kicked your butt!!

    not bad for the winter beater though.... too bad it only lasted 1 winter.
    2001 GTP- PT76 turbo, Intense Drag cars old engine, Stage 4 Intense turbo cam,FMIC,150 wet,Double roller timing chain,Diamond forged coated pistons 8:0:1,Diamond piston rings,Cryoed L32 connecting rods,Cryoed crank,Clevite77 main bearings,Clevite77 cam bearings,Clevite77 L32 rod bearings,ARP Everything, Intense/meizere true billet Flexplate,Intense Wilson UIM/LIM,Intense oil pressure kit,Cometic,OE-R lifters,Cryoed L67 block,ATI turbo dampner,80# inject,Weldon 2035 fp,Aero Fuel Rails,AL cradle
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  12. #12 Re: Good run, gone bad 
    GTP Level Member 2000GTP's Avatar
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    ahhh man that sucks!
    2000 GP GTP Black 2 Door AEM Meth Injection (100% Meth), 3.25" pulley, N* TB, PRJ Wires, Smoothflow Idlers, 42# injectors, Racetronix fuel pump, ZZP Headers, 1.8 Roller Rockers, Custom CAI, NGK TR6 Plugs, 180* Tstat, Custom Tuning by TUNE TIME PERFORMANCE
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  13. #13 Re: Good run, gone bad 
    The Blue One blueguy's Avatar
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    Quote Originally Posted by UR LOSN View Post
    not bad for the winter beater though.... too bad it only lasted 1 winter.
    That was my luck too...got a good deal and made almost a grand on it when a girl I worked with needed a car more than I did...damn I wish I had it since my GTP ain't running...
    Sold WBody's: '03 Blue GTP/'98 Green GTP/'98 Silver GT/'05 GXP
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  14. #14 Re: Good run, gone bad 
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    im curious how the head gasket went on a stock gtp? i always heard the stock headgaskets(if not ouched or removed) rarely if ever go bad and can go a long way b4 going bad.
    old setup-Z7 Turbo Kit w/T66, A2A I/C, stock cam & valvetrain/LS1 MAF/Ported 99TB/PowrTuner/AFC/Devils Own/LS1M Scanner/PRJ FP/42# Injs=12.3@118mph street tires -
    (Sold)BACK TO M90 Vs cam w/3.5" pulley/meth/25* timing+bolt-ons
    01 Z28 A4 HP-self-tuned, LTs, FTRA, 3600stall 12.3@112mph
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  15. #15 Re: Good run, gone bad 
    GTX Level Member Panther427's Avatar
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    That sucks. i have had none s/c 3800 go over 250,000+ miles with out blowing a head gasket. Very odd it went with the low amount of mods you had. im sorry to hear this UR LOSN
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  16. #16 Re: Good run, gone bad 
    GTX Level Member WhiteDevil's Avatar
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    Drop a tonawanda 638 in it and call it a day
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  17. #17 Re: Good run, gone bad 
    SE Level Member schreurs1's Avatar
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    they run the best before they blow.
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  18. #18 Re: Good run, gone bad 
    just call me john-o vailskier3's Avatar
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    what a bummer...

    2014 Camaro 2SS - stock, for now...
    SOLD but not forgotten - '07 GP Base SD Headers - hv3 - open cone - HPTUNERS user
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  19. #19 Re: Good run, gone bad 
    I live here. UR LOSN's Avatar
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    not really a bummer, otherwise I wouldnt have bought my new DD.
    2001 GTP- PT76 turbo, Intense Drag cars old engine, Stage 4 Intense turbo cam,FMIC,150 wet,Double roller timing chain,Diamond forged coated pistons 8:0:1,Diamond piston rings,Cryoed L32 connecting rods,Cryoed crank,Clevite77 main bearings,Clevite77 cam bearings,Clevite77 L32 rod bearings,ARP Everything, Intense/meizere true billet Flexplate,Intense Wilson UIM/LIM,Intense oil pressure kit,Cometic,OE-R lifters,Cryoed L67 block,ATI turbo dampner,80# inject,Weldon 2035 fp,Aero Fuel Rails,AL cradle
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  20. #20 Re: Good run, gone bad 
    GTX Level Member WhiteDevil's Avatar
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    5.3 swap it?

    you know you want to.
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