Thread: Worst Intake Gasket Failure Ever

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  1. #1 Worst Intake Gasket Failure Ever 
    I live here. TLSheff's Avatar
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    I bought 2003 Bonneville SSEi (supercharged 3800) from a kid that said he had been adding coolant for the last 5 months. He said it was leaking coolant and oil and he could only drive 5 miles before it would stall out. He said he was adding 1 gallon of coolant per week.



    draining the oil, which is probably more coolant than oil



    removed the filter



    It took about 30 minutes to drain all that crap out. It was some nasty stuff. I think I drained about 3-4 gallons from the engine. Now with the dis-assembly.



    Since the engine wasn't knocking yet, I decided I was going to try to save it and replace the intake gaskets. The first thing that comes off is the intake tube, and this the first thing I saw. Yes you are seeing that correctly, the "oil" level was all the way up into the supercharger and throttle body.



    leaking all the way into airbox



    Here is the supercharger filled with the oil/coolant solution.



    lifter valley was nasty



    bottom of the lower intake



    I was surprised to see the actual gasket failure wasn't even that bad compared to what I'm used to seeing.



    inside the valve covers



    rockers, what a mess....



    As this point, I’m wondering how in the world I’m going to clean this engine out. It was still running fine and it has a chance to be saved. I did some reading online about how to clean it out, but this was a pretty severe case. I did the unthinkable and took a pressure washer to the lifter valley and the heads. It cleaned up pretty nice. So after washing it out, I poured a gallon of oil all over the top of the engine to help flush any water out. I put the engine back together with new metal intake gaskets and metal coolant elbows. It fired right up and ran great. I did the first oil change after 5 minutes of running. The coolant looked the same as it did the first time from all the crap still in the oil pan. I did another oil change this time with 4 quarts oil and 1 quart of transmission fluid. I ran that mix for about 5 minutes and then drained again. This mix looked more like oil, but still not perfect. I did another oil change with oil and trans fluid and ran it for about 20 minutes. After this change, the oil looked like oil again with a slightly pink tint. I filled up the engine with its most current oil and it’s doing just great. I've logged over 1300 miles on the car since. I think I got pretty lucky.


    __________________________________________________

    Was posted on the GTP Facebook Group but for those that didn't see it.

    (Source) http://imgur.com/a/05azs

    Quote Originally Posted by AmericanSoldier View Post
    ...not scanning/monitoring your motor is like bangin a hooker and you just HOPE your not infected.
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  2. #2 Re: Worst Intake Gasket Failure Ever 
    Moderator dsmuts's Avatar
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    holy **** that's awesome lol
    98 GTP modded 1.9's, sd headers, 3.4", zzp 1.0 230K miles scrapped.
    04 Comp G zzp stb's, UMI ta's, Speedbuilt sways, bully flo heads, XP, zzp headers, fsic, thrasher shift kit, 60#, 2.6" corsa 2.5", Inferno hood
    01 gt z7 turbo tep trans zzp motor
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  3. #3 Re: Worst Intake Gasket Failure Ever 
    Turbo is the way to go. Fivefingerdeathpunch's Avatar
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    I think the reason it came out the intake is because it foamed up so bad, but thats minor compared to what was going on LOL.

    Crazy to see those pictures, glad its running great now.

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  4. #4 Re: Worst Intake Gasket Failure Ever 
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    2003 SSEi,
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  5. #5 Re: Worst Intake Gasket Failure Ever 
    Master-Breaker CapnBreakAlot's Avatar
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    Quote Originally Posted by dsmuts View Post
    holy **** that's awesome lol
    Awesome isn't the word I'd use.. haha. That is pretty crazy though.. Good luck with it.
    2001 Buick Regal GSE - S1X - Blue 90# springs - TOG's - Devils Own Water/Methanol kit - 80s - E85 - ZZP 3" dual catback - 2.7 - 23* - N* TB - LQ4 MAF - Gen V - TEP Stage 3 Trans - 3.29s - Self tuned with HPT - 347/423 --- Sold
    ​2013 5.slow F150 - MAK catless Y pipe - Roush catback - self tuned with HPT
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  6. #6 Re: Worst Intake Gasket Failure Ever 
    GrandPrix Junkie machinegunsquid's Avatar
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    That's where all the cookies have gone, into the new SSEI and Creme!

    "**** bills. You can live in your car but you can't race your house" -dsmuts
    Want her to stop when she's not looking karate chop her in her crotch that should quiet her for a bit or at the very least put a smile on your face -REDCOMPG
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  7. #7 Re: Worst Intake Gasket Failure Ever 
    GTX Level Member 87IROCZOWNER69's Avatar
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    If I would have opened it up and seen that I probably would have just sat down and cried. lol
    Quote Originally Posted by BoostenGTP View Post
    Do it Dan. Be a Grand Prix owner. Be an Asshole.
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  8. #8 Re: Worst Intake Gasket Failure Ever 
    GrandPrix Junkie
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    I honestly can't see how it didn't spin every bearing in the motor, I really can't. I hope it holds together for you. Looks like a nice Bonnie other than the front end.
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  9. #9 Re: Worst Intake Gasket Failure Ever 
    Killa Bee Scottydoggs's Avatar
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    that engine is so lucky to be alive. amazing.

    i guess you got it for super cheap? car looks pretty damn good. other then the bad lim gaskets.

    98 Buick Regal GS, F body brakes, Caddy STS wheels, tinted tails L36 bottom end, lightly ported heads, 1.95 roller rockers, headers, gen 5 N* 3.0 pulley, FSIC, 42 lb injectors, a BrandonHall rebuilt trans, DHP tuned and AEM water/Meth injection https://goo.gl/gpV5kW
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  10. #10 Re: Worst Intake Gasket Failure Ever 
    I live here. ericspecullaas's Avatar
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    TLSheff is the luckest man in the world right now. and here i thought mine was bad lol you had to go and beat me hahaha
    im a cookie again yay me
    Quote Originally Posted by Bio248 View Post
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  11. #11 Re: Worst Intake Gasket Failure Ever 
    Donating Users 16MustangVet's Avatar
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    No way in hell id keep that engine after all the coolant in it. If its still running its just a matter or time..........

    Amazing what stupid people can do to engines though!!!!
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  12. #12 Re: Worst Intake Gasket Failure Ever 
    I live here. theaceofspades's Avatar
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    Your so lucky
    Quote Originally Posted by theaceofspades View Post
    I now own a stance car parts I just like them DICKS
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  13. #13 Re: Worst Intake Gasket Failure Ever 
    GTX Level Member 98buicksupercharged's Avatar
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    That is awesome man! Congrats
    2001 sliver gtp her name is Reagan
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  14. #14 Re: Worst Intake Gasket Failure Ever 
    GTP Level Member LeadfootCJ7's Avatar
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    Awesome!

    Go trade it in before it blows!
    2007 Grand Prix GXP;2002 Camaro Z28 - tune, CAI, and exhaust
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  15. #15 Re: Worst Intake Gasket Failure Ever 
    Turbo is the way to go. Fivefingerdeathpunch's Avatar
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    The OP TLsheff didnt buy it, he's just posting the pictures and stuff in a thread.

    Read the link posted in post #4.

    SMGPFC Member #1
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  16. #16 Re: Worst Intake Gasket Failure Ever 
    GTX Level Member QUICKSILVER462's Avatar
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    I did a head gasket on a 76 Buick 350 that had oil like a vanilla milkshake, after having to pull the motor to get to the head bolts in the rear of the engine, and reassembling everything back correct, the darn thing ran 3 more years I know of in high school, and who knows how long after.
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  17. #17 Re: Worst Intake Gasket Failure Ever 
    GTP Level Member indygrandprix's Avatar
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    That's crazy that thing doesn't have a knock.
    Quote Originally Posted by BillBoost37 View Post
    I went NA when a whore left -$300 in my bank account.
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  18. #18 Re: Worst Intake Gasket Failure Ever 
    GTP Level Member 231FUN's Avatar
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    Quote Originally Posted by Fivefingerdeathpunch View Post
    The OP TLsheff didnt buy it, he's just posting the pictures and stuff in a thread.

    Read the link posted in post #4.
    Not sure if I'm suprised more by that coolant or by how many people fail at reading...LOL!
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  19. #19 Re: Worst Intake Gasket Failure Ever 
    I live here. TLSheff's Avatar
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    HAHA Yeah, definitely not mine. Altho, if I could get one on the cheap like that and it still runs, I would buy it and restore it like this and see how long it lasted before throwing in a junkyard motor lol.

    I just came across it on the FB Group and thought I would share for all the L67 lovers out there. I mean I had a small gasket failure, didn't even make the motor act up, but I replaced the factory gaskets anyways at 74k like a good owner, and changed the oil and kept an eye on the motor and everything was fine, but still spun a bearing at 83k. Maybe this one will hold together for him, but I wouldn't be surprised if he has problems down the road. I couldn't find the origin thread, but figured someone would know whose it was.

    Post# 4, good job man, giggled my way through that thread.

    Quote Originally Posted by AmericanSoldier View Post
    ...not scanning/monitoring your motor is like bangin a hooker and you just HOPE your not infected.
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  20. #20 Re: Worst Intake Gasket Failure Ever 
    GXP Level Member coolone's Avatar
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    That's just sickening! Crazy that it runs afterward, but could be be of those 1 - 1,000,000 that you just can't kill!
    lol
    Overkill BBC Cam, YT 1.8 RR's, Rhodes Lifters, STGII Heads, GenV, Pacesetters, 3" Exh to Tips, TEP Trans. N*, ID 75# injectors/E85 coming soon
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