so i took apart the whole engine today because there was a loud knock noise coming from the inside of the engine. I had KR up around 14, and i am thinking i overboosted the engine. I had the P0121 code also. I was running a 2.8 Pulley, maybe i should of been going to the 3.0 or 3.1. i always use 93 octane. Here are my mods, and attached is a copy of my power tuners bin file. Turns out 6 Chipped Pistons. Pictures Below
Triple Edge ported Gen III (inlet and outlet, setup for an I/C)Trannyman
INTENSE Supercharger coupling
INTENSE PCM
INTENSE™ Stage 1X Blower Cam, duration @ .050": 210?/221?, lobe lifts: .321"/.329", valve lifts with 1.60:1 rocker arms: .514"/.526", lobe separation angle: 115?, intake centerline: 111?
1.6 Roller Rockers 3rd gen
LS6 105#
INTENSE Oil Restricted Pushrods 5/16 X .083 X 7.50
Comp Cam Lifters
Rollermaster Timing Chain Set
ZZP Valve Locks and Retainers
42.5# Flow matched
Walbro 255lph Fuel Pump
MSP CAI
Casper's Timing Commander
ZZP Voltage booster
MSD Ignition Wires
Sprint Tech springs
TOG headers back to a Thrush glasspack and Borla Pro XS mufflers with singe rolled tip
Performance Tranny Rebuild 10k Miles Ago(Hardened parts, shift kit)